Recent content by 340_dart_power

  1. 340_dart_power

    Supercuda's on the way back...after18 years!

    A continuing work of art, Sir; beautiful to see and appreciate.
  2. 340_dart_power

    Supercuda's on the way back...after18 years!

    Beautiful work, Sir; very nice and thanks for sharing.
  3. 340_dart_power

    The 340 is out....again.....

    RGR that; I am just so glad to have it back and running properly.
  4. 340_dart_power

    The 340 is out....again.....

    Well, apparently the missing plug was the problem. The 340 is back in and running strongly. Here's a video from Wednesday of this week:
  5. 340_dart_power

    The 340 is out....again.....

    Good copy, All. I'll chat with the shop next week about the additional concerns and advise. Thanks for the input, as always. I'd really like to get the Dodge back and on the road again.
  6. 340_dart_power

    The 340 is out....again.....

    UPDATE: Received a call from the shop yesterday and the real issue has been identified as a missing freeze plug. Apparently this had been removed by the first engine shop I had hired to do the rebuild and was never replaced. It's not one which comes in a rebuild kit of plugs, and shouldn't...
  7. 340_dart_power

    The 340 is out....again.....

    (Shakes his aching head...)
  8. 340_dart_power

    The 340 is out....again.....

    Good discussion, thanks for the input as always. I'll ask the shop about the mains being drilled completely.
  9. 340_dart_power

    The 340 is out....again.....

    So, it appears we have diagnosed and identified the problem. The camshaft bearings which were used were too narrow for the application in my 340. They are 1/4 inch smaller/narrower than the ones which should have gone into the build. Instead of riding on the layer of oil, the camshaft as it spun...
  10. 340_dart_power

    The 340 is out....again.....

    Gentlemen, thank you all for your input. I am the first to admit that I do not have the technical expertise that I'd like to have, and in this area I appreciate any and all relevant input. FYI, I've taken your comments to my garage guys in printed format and have asked them to review your...
  11. 340_dart_power

    The 340 is out....again.....

    Latest rebuild resulted in the same damage to the camshaft bearings after being run for awhile, so the block and heads are back at the machine shop. The current suspicion is that the Edelbrock Performance heads may be to blame in some fashion. No end in sight at this point....
  12. 340_dart_power

    The 340 is out....again.....

    That I do not know. I believe the shop which rebuilt it originally just didn't have the Mopar engine knowledge base they thought they had. Typically they are rebuilding Chevrolet/GM/Ford engines, and my guess is that they just missed some of the differences involved in rebuilding the 340. The...
  13. 340_dart_power

    The 340 is out....again.....

    The camshaft bearings were destroyed. The camshaft dug down into them instead of riding along on top of them. It also turned out that the old shop did an overbore of .033 instead of .030, which wasn't a really good combination to have with the .030 pistons. It now has an overbore of .040 with...
  14. 340_dart_power

    The 340 is out....again.....

    It was a stock pickup. The oil pressure gauge consistently showed great pressure throughout the driving time before the knock showed up and ruined the party. It gave me no indication there was a problem brewing.
  15. 340_dart_power

    The 340 is out....again.....

    LOL, no worries, Gents; I do appreciate the discussion, not taking the heat at all. On a side note, here's some photos of the new lower radiator support from XV Motorsports, in place on the Dart:
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