Nor-Cal '73 Swinger

I was dicking around with the fuel line from the pump to carb the other night & when I was done thought all was fine. Jumped in the car yesterday to go shoot the breeze with Bad440 Mike & had myself a good old fashioned fuel leak. Didn't want to change clothes yesterday so I left it for today & went to Mike's in the truck. Pulled the secondary bowl off today & cleaned the needle & seat & that fixed the problem but while I was poking around I noticed a vacuum cap severely cracked & obviously leaking badly. Luckily, I found a spare in the toolbox & when I capped it off it took care of a noticeable off idle bog I thought was a tuning issue & the throttle response is now absolutely tremendous. I went out & pissed the new neighbors off for about 20 minutes & couldn't believe the difference that tiny vacuum cap made.

I have to say that the little 318 is now kicking way more *** than I had imagined when I first set out to wake it up. I've now amassed all the components for my 8.75 swap with 3:23 SG & have that on the radar with the TF-2 kit for the tranny in the next 2-3 weeks. I'm excited to get those done.

On the other hand, I still haven't gotten the center console brackets welded in yet & I have the template, mounting brackets, complete console, shifter & linkage in the garage collecting dust. I really need to get that back on track. Hopefully soon. I've let being so far out be my excuse for not making progress. I need to get my eye back on the ball.

Also I picked up a Mopar Performance air cleaner from Mike & cleaned it up & threw it on today. Not sure if I like it better than the Moroso that was there before. Maybe it will grow on me. What do you guys think? Keep it, or go back to the Moroso?
figured the old ocd would make you keep it on there...lol looks good though...