Another clutch not completely disengaging thread

Hey everyone thanks for the replies, i just spent another 3 hours trying to vacum bleed, pressure bleed, played around with the MC rod adjustment (again) and nothing. It is still exactly the same, managed to have a look at pressure plate and all looks to be working fine, just not disengaging enough.
So before i remove the trans for the 6th or 7th time (lost count now) would it be worth trying a larger bore MC like say 7/8"?
I have a wilwood master and slave, on my car. I get 1.3 inch on the master and 1.25 on the slave. I would do as Del said and set it up on the bench. Can you call the maker of the bearing and find out what the stroke is supposed to be?

Website says it has a max travel of 3/4", of which im getting approximately 3/8", and the MC (3/4" bore with 1.4" stroke is fully stroked).