Slow, Driving Rustoration 1972 Dart

Well today was the day. Of not much progress.

Started a little after 9 am and had the transmission loose and slid back by a little after noon. I managed to do it without taking the exhaust down. I may have to loosen the driver side to get everything reinstalled though.
20221231_121204.jpg

It was a rusted plug causing the coolant leak as expected. The passenger side one looked good but I removed it as well. The water channel was packed with rusty debris so I flushed a couple of gallons through the block to get some of it out.

20221231_124535.jpg

20221231_124544.jpg

20221231_132442.jpg

Then the fun started. I hadn't preordered the plugs, thinking they would be readily available. I went to every parts store in town, Oreilly, AZ, Advance, and NAPA. I looked up part numbers on rock auto and they were not right. Nobody had any 1 5/8" plugs, brass or otherwise.

Finally gave up and cleaned up my brother-in-laws shop and went home about 4. I ordered a set from O'Reilly in brass that will be here Monday. I also ordered 2 of the rubber expansion style just in case.

20221231_132442.jpg