Here is one change I have made in preparation for continuation of dyno testing. Air door adjustments by bending the metal flap is not a good approach IMO. So I made an adjustable screw using a cut #4 screw nut coupler, a #4 set screw and a jam nut. I used solder to attach it to the existing...
Do you have any info you can share on the anti-siphon feature of the CS? We had an issue with fuel being pulled out of the squirters. Would like to replicate that.
Also, can you share tuning details of any high HP setups you have been involved with? Jets, rods, bleeds, door opening etc? Thank you
We played around with the sec high speed bleeds. Went from 36 to 38 then 42. It went too lean, the biggest jets we had were .156, which made most power after re-sizing HSB back to .036. Found out we needed the air door open as much as practical, which pulled less fuel into the engine. We have...
I was not allowed to make permanent changes to the TQ, i.e. could only do sec air door opening, jets, rods etc. The sec butterflies were left at 86 deg opening. I completely ignored all advice on the sec air door; in fact I removed the stop so it would open all the way at .960". That was a...
They have those. I noticed them but was unsure of their function. On the 2nd Tquad which has the enlarged venturi but still has the 2 boosters, idle, low-speed, and the transition between works very well, just as good as stock. I'm wondering if playing with those would be better when the car is...
From my observations on the dyno, I feel the single booster mod is not the best approach for low speed manners. It will help WOT power however.
All other mods did not affect low speed in a significant way
I used the Edelbrock larger fuel fitting p/n 8090 along with a 3/8" barb adapter, but did not drill the feed in the top.
I had the .110" needle and seats
I did quite a lot of tuning. Maybe 20+ pulls of stuff that didn't work. Sec air valve didn't really care on # of turns, that is more of a dynamic thing (transition to WOT etc). Air door much past .800 didn't work regardless of jet size. Sec butterfly blades were 86 to 88 deg.
I needed something like that. Video showed fuel being pulled out of the squirters. We ended up with a BB and ink pen spring on top of the squirter valve to counteract.
Video of carb in action:
So, got some semi final results. Its semi final because we didnt finish, a mechanical failure prevented me from testing one last carb. But will finish in the coming spring. To recap and clarify, used a 950 Holley Ultra HP 0-80805, an Everyday Performance prepped Stage 2 800 cfm Qjet and a "950"...