my5thmopar
Life Long MOPAR Owner
I removed the RMVB from my 76 727. I installed a 71 VB from my spare 904. It has a part time KD and I added a TF2. The governor in tail-shaft wasn’t removed. Reverse and drive is firm and immediate. The 1-2 is hard and will bark tires. 3rd will work if I go to neutral and back to 3rd. It seems it will drop back to 2nd with the slightest throttle. I went middle of the hole drilling, the ball was left in, accumulator is not blocked. Orifice pLug installed. I’m thinking I messed up the shuttle valve grinding or got spring wrong place. I adjusted the bands per the TransGo instructions. I overfilled just for testing and back to correct level. It’s not fluid level...I’ve had Mopars since the 70s.
Anything else I can try before I pull the pan?
I’m going to check Lokar shifter and Lokar KD cable adjustments today. Thanks Craig
Anything else I can try before I pull the pan?
I’m going to check Lokar shifter and Lokar KD cable adjustments today. Thanks Craig
so get busy haha.














