540slant6
Mopar SB Ripper
Ok guys, some history. My stock internals 318 blew a head gasket at Mason Dixon show in MD back in June. Still ran but dumped a bunch of milky oil into the motor.
Last month I drained the oil and put on a set of decked 360 heads on it. No other changes to the setup. Put a fresh filter and new 10w30 non synthetic in it. The motor runs great, good temperature and oil pressure.
Only issue is that smoke or steam appears to be coming out of the breather. Not terrible but noticeable. I'm thinking some of the milky oil with the water in it is burning off and exiting through the breather. Any thoughts?
I was going to let the car get warm and change the oil again to see if anything changes. I'm familiar with the open versus closed breather debate but there was no smoke before the head gasket blew.
Any help is much appreciated, thanks fellars.
Last month I drained the oil and put on a set of decked 360 heads on it. No other changes to the setup. Put a fresh filter and new 10w30 non synthetic in it. The motor runs great, good temperature and oil pressure.
Only issue is that smoke or steam appears to be coming out of the breather. Not terrible but noticeable. I'm thinking some of the milky oil with the water in it is burning off and exiting through the breather. Any thoughts?
I was going to let the car get warm and change the oil again to see if anything changes. I'm familiar with the open versus closed breather debate but there was no smoke before the head gasket blew.
Any help is much appreciated, thanks fellars.















